mking
10-29-2006, 11:44 PM
Tuning JLTOs
I thought I would share my recent experiences tuning a JLTO, from out of the box to a Fray style racer.
The track: 4x8 4 lane routed track with Magnatech braid instead of rail (Thundertrack).
Timing: diodes with Greg Braun’s software
The Car: JLTO chassis (grey, not the black R1 chassis). No body, pick up shoe glued in for testing.
Out of the box. Could not make a single lap without de-slotting. Rear axles holes particularly sloppy; lots of rear wheel hop.
Restricted pickup shoe travel with heat shrink tubing. Been using 5/64 tubing but recently switched to 1/16. The 5/64 size slips on and then must be heated to stay in place, the 1/16 can be forced onto the shoe, and stays in place without needing to be shrunk. Put o-rings on stock hubs, really lowering the front end (about 0.320). Best lap time: 8.3 seconds. Still hard to control.
oops! the heat shrink tubing is 1/16, not the 1/8 i first reported
Replaced stock rear tires with Weird Jack’s tuffy silicons (from a bag of rejects). Best lap time: 7.2 seconds. 15.3% improvement over Step #2.
Replace rear axle with a 1 5/16 wide drill rod axle; wire size 50 (that’s 0.070; a big step up from stock axles, which are about 0.062). I buy drill rod in various sizes, and cut axles with a cutoff disk and a dremel. I use whatever size I need to eliminate all slop. Usually that means I need to enlarge one or more of the rear axle holes. I do this by chucking the right size axle into another dremel (I have several dremels to avoid having to keep replacing bits) and running the axle into the axle holes. If the hole really needs to be opened up, I use some Simi chrome or rubbing compound. This is the hardest part of my tuning, as you want the axle to just fit. No slop, but no grab either. A good fitting axle will really reduce friction. It usually takes me about 10-15 minutes for this step, stopping frequently to avoid over boring the axle holes. 0.0625 axels (1/16 drill rod) will work with stock hubs (pressed on with a wheel press). If I use a larger axles, I either use different hubs, or I ream out the hole in the stock hub (I have had good luck using the axle chucked into the dremel; with the wheel holder removed from my wheel press, the JLTO hub fits in the opening in the wheel press, and I can use the wheel press to hold the hub while I ream it, letting me ream a reasonably straight hole). Then I use black max (rubberized superglue) to secure the hubs to the axle. Just a note, the replacement axle is smooth, and I usually have no trouble with the crown gear spinning. The replacement axles are larger than the stock axle, and the crown gear holds fine to the larger smooth axle (the stock axles have splines). I have screwed up a chassis enlarging the rear axle holes, but if I do I can usually just use the next larger size axle material. Then I use a wire brush (in another dremel of course!) to buff the gears, with the brushes and magnets removed, and the gear plate in place (with the gear clamp on, to keep the middle gear from shooting off to parts unknown). I am careful not to remove too much material from the plastic gears. Some people use Simi chrome for this step, I have found the wire brush works well, and is a lot less messy. After this step, the best lap time was 6.77 seconds, and the chassis was A LOT more predictable to drive. That’s a 22.5% improvement over Step 2, and a 6.35% improvement over Step 3 (diminishing returns!).
Added Fray style independent fronts (wider; 1 5/16 and weighted). I used home made fronts, you can buy them for $6-8. Mine cost about $2.25; 1/16 hollow brass tubing ($0.60 for 12 inches at hobby stores), standard flat head sewing pins ($1.50 per hundred at Walmart), stock chrome TJET hubs from
I thought I would share my recent experiences tuning a JLTO, from out of the box to a Fray style racer.
The track: 4x8 4 lane routed track with Magnatech braid instead of rail (Thundertrack).
Timing: diodes with Greg Braun’s software
The Car: JLTO chassis (grey, not the black R1 chassis). No body, pick up shoe glued in for testing.
Out of the box. Could not make a single lap without de-slotting. Rear axles holes particularly sloppy; lots of rear wheel hop.
Restricted pickup shoe travel with heat shrink tubing. Been using 5/64 tubing but recently switched to 1/16. The 5/64 size slips on and then must be heated to stay in place, the 1/16 can be forced onto the shoe, and stays in place without needing to be shrunk. Put o-rings on stock hubs, really lowering the front end (about 0.320). Best lap time: 8.3 seconds. Still hard to control.
oops! the heat shrink tubing is 1/16, not the 1/8 i first reported
Replaced stock rear tires with Weird Jack’s tuffy silicons (from a bag of rejects). Best lap time: 7.2 seconds. 15.3% improvement over Step #2.
Replace rear axle with a 1 5/16 wide drill rod axle; wire size 50 (that’s 0.070; a big step up from stock axles, which are about 0.062). I buy drill rod in various sizes, and cut axles with a cutoff disk and a dremel. I use whatever size I need to eliminate all slop. Usually that means I need to enlarge one or more of the rear axle holes. I do this by chucking the right size axle into another dremel (I have several dremels to avoid having to keep replacing bits) and running the axle into the axle holes. If the hole really needs to be opened up, I use some Simi chrome or rubbing compound. This is the hardest part of my tuning, as you want the axle to just fit. No slop, but no grab either. A good fitting axle will really reduce friction. It usually takes me about 10-15 minutes for this step, stopping frequently to avoid over boring the axle holes. 0.0625 axels (1/16 drill rod) will work with stock hubs (pressed on with a wheel press). If I use a larger axles, I either use different hubs, or I ream out the hole in the stock hub (I have had good luck using the axle chucked into the dremel; with the wheel holder removed from my wheel press, the JLTO hub fits in the opening in the wheel press, and I can use the wheel press to hold the hub while I ream it, letting me ream a reasonably straight hole). Then I use black max (rubberized superglue) to secure the hubs to the axle. Just a note, the replacement axle is smooth, and I usually have no trouble with the crown gear spinning. The replacement axles are larger than the stock axle, and the crown gear holds fine to the larger smooth axle (the stock axles have splines). I have screwed up a chassis enlarging the rear axle holes, but if I do I can usually just use the next larger size axle material. Then I use a wire brush (in another dremel of course!) to buff the gears, with the brushes and magnets removed, and the gear plate in place (with the gear clamp on, to keep the middle gear from shooting off to parts unknown). I am careful not to remove too much material from the plastic gears. Some people use Simi chrome for this step, I have found the wire brush works well, and is a lot less messy. After this step, the best lap time was 6.77 seconds, and the chassis was A LOT more predictable to drive. That’s a 22.5% improvement over Step 2, and a 6.35% improvement over Step 3 (diminishing returns!).
Added Fray style independent fronts (wider; 1 5/16 and weighted). I used home made fronts, you can buy them for $6-8. Mine cost about $2.25; 1/16 hollow brass tubing ($0.60 for 12 inches at hobby stores), standard flat head sewing pins ($1.50 per hundred at Walmart), stock chrome TJET hubs from